Part 2 (H)
Recovery, Spacecraft Redefinition, and First Manned Apollo Flight
January 1968
1968
January 2
MSC called to the attention of North American Rockwell the
number of discrepancies found at KSC that could have been found at Downey before
hardware shipment. In an effort to reduce the discrepancies North American was
requested to obtain and use the KSC receiving inspection criteria as a guide for
shipping inspections. It was also suggested that the possibility of sending a
few key inspectors to KSC for periods of three to six months to gain additional
experience might be investigated.
Ltr., Kenneth S. Kleinknecht, MSC, to Dale D. Myers, North American Rockwell,
Jan. 2, 1968.
January 5
ASPO Manager George M. Low discussed with Rocco Petrone of KSC
the problem of high humidity levels within the spacecraft-lunar module adapter.
Petrone advised that several changes had been made to alleviate the problem: air
conditioning in the SLA and the instrument unit would remain on during
propellant loading; and the rate of air flow into the SLA was increased. Also,
technicians at the Cape had designed a tygon tube to be installed to bring dry
air into the LM descent engine bell, should this added precaution prove
necessary. With these changes, Low felt confident that the humidity problem had
been resolved.
Memo for the Record, Low, "SLA humidity," Jan. 8, 1968.
January 5
Bellcomm engineers presented to NASA a proposed plan for lunar
exploration during the period from the first lunar landing through the
mid-1970s. The proposed program - based upon what the company termed
"reasonable" assumptions concerning hardware capabilities, scientific
objectives, launch rates, and relationships to other programs - was divided into
four distinct phases:
- an Apollo phase using existing vehicles,
- a lunar exploration phase employing an extended LM with increased payload
and longer staytime,
- a lunar orbital survey and exploration phase using remote sensors and
photographic equipment on a polar orbit flight, and
- a lunar surface rendezvous and exploration phase using an unmanned LM to
deposit the increased scientific equipment and expendables necessary to extend
Apollo's manned lunar capability to two-week duration.
N. W. Hinners et
al., Bellcomm Technical Memo 68-1012-1,"A Lunar Exploration Program," Jan. 5,
1968.
January 5
Apollo Special Task Team (ASTT) Director Eberhard F. M. Rees,
Martin L. Raines, and Ralph Taeuber of MSC, and J. McNamara, North American
Rockwell, visited Rocketdyne Division to review the status of the LM ascent
engine backup program. The presentation was made by Steve Domokos.
The group was favorably impressed and felt that there was every indication
that the Rocketdyne injectors would meet the LM requirements. ASTT recommended
that MSC establish a board, chaired by the Chief of the Propulsion and Power
Division and including one MSFC propulsion engineer, one MSFC manufacturing
specialist, and other MSC personnel as required to provide a recommendation to
ASPO of the ascent engine for LM-3.
Memo, Raines to Manager, ASPO, "Trip Report - Rocketdyne - January 5, 1968,"
Jan 8, 1968.
January 8
NASA Associate Administrator for Manned Space Flight George E.
Mueller directed MSC Director Robert R. Gilruth to establish a task team to
investigate why, in light of extreme precautions taken early in the program, the
problem of stress corrosion in the LM was being encountered at such a late stage
in Apollo. The problem, Mueller stressed, had been discovered at a most critical
point in the program - the launch of the first LM was imminent and two
subsequent vehicles were already well along in factory checkout. Any resultant
slips in the LM program would seriously impact overall Apollo schedules. Gilruth
replied he believed that such a team was not required. He affirmed that the
reviews undertaken with the contractors in 1964 to guard against just these
problems had proved inadequate when judged against present program demands. "The
answer simply is that the job was not handled properly on the last go-round."
Ltrs., Mueller to Gilruth, Jan. 8, 1968; Gilruth to Mueller, Jan. 18, 1968.
January 9
George E. Mueller, NASA OMSF, in a letter to MSC Director
Robert R. Gilruth, summarized a number of key Apollo program decisions required
in order to emphasize the urgency of priority action in preparations necessary
to certify the Apollo system design for manned flight. Mueller listed five
items:
- Assuming a successful flight of Apollo 5, the LM design must be certified
ready for manned flight on AS-503.
- A successful test firing of SM 102 at Cape Kennedy in January, in addition
to the success of Apollo 4, would permit certification of the SM propulsion
system for manned flight on AS-205.
- A successful launch vehicle test of AS-502 (Apollo 6) would require that
the Saturn V design be certified ready for manned flight by early April 1968.
- A decision to certify the Block II CM design for manned flight should be
essentially complete by early May 1968.
- Launch Complex 34 design should be certified for manned flight no later
than early June 1968.
Ltr., Mueller to Gilruth, Jan. 9, 1968.
January 11
Apollo Data Coordination Chief Howard W. Tindall, Jr.,
summarized mission planning for the first two hours on the lunar surface. That
period, he said, would be devoted to checking out spacecraft systems and
preparing for launch (in effect simulating the final two hours before liftoff).
This procedure embodied several important benefits. As a pre-ascent simulation,
it would afford an early indication of any problems in the checkout routine.
More importantly, the initial checkout procedure would prepare the LM for
takeoff at the end of the CSM's first revolution should some emergency situation
require such an immediate flight abort.
Memo, Tindall to distr., "First 2 hours on the moon is a countdown to launch
- simulated or real thing," Jan. 11, 1968.
January 11
A Parachute Test Vehicle (PTV) test failed at El Centro,
Calif. The PTV was released from a B-52 aircraft at 15,240 meters and the drogue
chute programmer was actuated by a static line connected to the aircraft. One
drogue chute appeared to fail upon deployment, followed by failure of the second
drogue seven seconds later. Disreefing of these drogues normally occurred at 8
seconds after deployment with disconnect at deployment at plus 18 seconds. The
main chute programmer deployed and was effective for only 14 out of the expected
40 seconds' duration. This action was followed by normal deployment of one main
parachute, which failed, followed by the second main parachute as programmed
after four-tenths of a second, which also failed. The main chute failure was
observed from the ground and the emergency parachute system deployment was
commanded but also failed because of high dynamic pressure, allowing the PTV to
impact and be destroyed. Investigation was under way and MSC personnel were en
route to El Centro and Northrop-Ventura to determine the cause and to effect a
solution.
TWX, George M. Low, MSC, to NASA Hq., Attn: Apollo Program Director, Jan. 11,
1968.
January 11
CSM Manager Kenneth S. Kleinknecht wrote his counterpart at
North American Rockwell, Dale D. Myers, to express concern about NR's seeming
inability to implement configuration control of flight hardware and ground
support equipment. Some progress had been made recently, Kleinknecht observed,
but many steps still had to be taken to achieve effective configuration
management on the CSM. The MSC chief pointed especially to North American's
inability to ensure that final hardware matched that set forth in engineering
documents, a weakness inherent in the separate functions of manufacturing:
planning, fabrication, assembly and rework. MSC recommended a check procedure of
comparing part numbers of installed equipment to the "as designed" parts list.
"In short," Kleinknecht concluded, "I think that we should tolerate no further
delay in establishing a simple 'as built' versus 'as designed' checking
function, beginning with and including the first manned spacecraft."
North American began a more nearly complete engineering order accountability
system, which provided an acceptable method of verifying the "as designed" to
the "as built" configuration of each spacecraft. This system was planned to be
applicable by the Flight Readiness Review on spacecraft 104 and on subsequent
spacecraft at earlier points.
Ltrs., Kleinknecht to Myers, Jan. 11, 1968; Myers to Kleinknecht, Feb. 13,
1968.
January 13
The Senior Flammability Review Board met at MSC with Chairman
Robert R. Gilruth, George M. Low, Maxime A. Faget, Aleck C. Bond, Charles A.
Berry, Donald K. Slayton, Christopher C. Kraft, Jr., Kenneth S. Kleinknecht, all
of MSC, and George Jeffs of North American Rockwell participating. The meeting
summary reported that a 60-percent-oxygen and 40-percent-nitrogen atmosphere was
acceptable from a crew physiological standpoint. The requirement for crew
prebreathing before launch was not dependent upon launching with the atmosphere.
Operationally, the crew could remove their helmets and gloves following orbital
insertion and verification of the integrity of the cabin and its environmental
control system; oxygen leakage would be allowed to enrich the crew compartment
atmosphere.
On January 25, Berry, MSC Director of Medical Research and Operations, mote
Gilruth: "We do not concur in the stated finding of the Board that a 60 per cent
oxygen, 40 per cent nitrogen atmosphere is acceptable from a crew physiological
standpoint. While it is true that a 60% oxygen, 40% nitrogen atmosphere at 5.6
psi [3.9 newtons per sq cm] should result in a cabin atmosphere physiologically
equivalent to sea level conditions, this will not be the case in a spacecraft
launched with a 60% oxygen, 40% nitrogen atmosphere to which no oxygen is added
except by normal operation of the cabin regulator. Oxygen will be metabolized by
the crew at a much greater rate than nitrogen will be leaking from the
spacecraft. Assuming a case in which cabin relief valve seats at 6 psi [4.1
newtons per sq cm] and the cabin regulator does not begin adding oxygen until
4.8 psi [3.3 newtons per sq cm], the cabin atmosphere would then consist of
approximately 49% oxygen. This is physiologically equivalent to a 12,000-foot
[3,700-meter] altitude in air. It would then take approximately 50 hours at the
nominal cabin leak rate for the cabin regulator to enrich the mixture to a sea
level equivalent."
"Senior Flammability Review Board Meeting," MSC, Jan. 13, 1968; memo, Berry
to Gilruth, "Senior Flammability Review Board Meeting, January 13, 1968," Jan.
25, 1968.
January 13
ASPO Manager George M. Low outlined for the NASA Apollo
Program Director MSC plans to static-fire the service propulsion system (SPS) as
a complete unit. Houston officials maintained that at least one firing of such a
complete system was necessary to prove the adequacy of all SPS manufacturing,
assembly, and testing. However, because of several potential adverse effects
that might accrue to testing the first such available system (that for the 101
SM), MSC proposed to test-fire the 102 unit and interpret those results -
including any possible damage to the SM structure itself - before making a final
decision on whether to proceed with a ground firing of the actual flight
hardware before flight.
Memo, Low to NASA Hq., Attn: Samuel C. Phillips, "Requirements for static
firing of Apollo service propulsion subsystem," Jan. 13, 1968.
January 15
George E. Mueller, NASA Associate Administrator for Manned
Space Flight, summarized for Administrator James E. Webb recent program progress
in Apollo. Preparations were under way toward the revised January 22 launch date
for Apollo 5. Delays had resulted primarily from difficulties with hypergolic
loading and contamination problems, but propellant loading had been completed
several days earlier. Target for the countdown demonstration test was January
19. At Buffalo, N.Y., the NASA stability team assisted Bell Aerospace Co. in
tackling the LM ascent engine instability problem. Post-test analysis of the
qualification engine had revealed gouging of the chamber wall near the injector
face. Bell engineers were assessing the amount of requalification testing that
would be required and continued their testing on reworked engines, seeking to
find the cause of previous engine instabilities. Meanwhile, the backup injector
program at Rocketdyne Division was proceeding extremely well. Tests employing
fuel film cooling had produced increased engine performance within acceptable
chamber erosion limits. Altitude tests were scheduled to follow within a few
weeks.
Memo, Mueller to Administrator and Deputy Administrator, "Manned Space Flight
Report - January 15, 1968."
January 17
Eberhard Rees, Director of the Apollo Special Task Team at
North American Rockwell's Downey plant, wrote ASPO Manager George Low outlining
what he termed "serious quality and reliability resources deficiencies" and
proposed several steps to bolster NASA's manpower in these areas. Specifically,
Rees cited the immediate need for additional manpower (primarily through General
Electric) to make vendor surveys, test failure assessments, and specification
review and analysis and establish minimum inspection points. In addition, Rees
said, many areas were almost totally lacking in coverage by the government, such
as monitoring qualification tests, receiving inspections, pre-installation test,
and many manufacturing operations. He urged Low to reassess his requirements in
Houston to determine how many persons MSC might contribute (along with those
from MSFC and GE) to plug these vital areas.
Ltr., Rees to Low, Jan. 17, 1968.
January 17
Eberhard Rees, Apollo Special Task Team chief at North
American Rockwell, participated in a failure review at Northrop-Ventura of the
recent parachute test failure (see January 11) and in development of a revised
test plan. Others at the review included Dale Myers and Norman Ryker from North
American and W. Gasich and W. Steyer, General Manager and Apollo Program Manager
at Northrop-Ventura. Those at the review put together a revised drop test
program that resulted in only a two-week schedule delay because of the failure.
Repair of the parachute test vehicle was under way. Meantime, tests would
continue, employing bomb and boilerplate devices. Also, Rees decided to
establish a Flight Readiness Review Board (headed by Joseph Kotanchik of MSC) to
approve each drop test, and Northrop officials had established an internal
review board to review test engineering and planning and were tightening their
inspection and quality control areas.
Memo, Rees to Manager, ASPO, "Trip Report to Northrop-Ventura on January 17,
1968," Jan. 19, 1968; ltr., Kenneth S. Kleinknecht, MSC, to Myers, Jan. 19,
1968.
January 18
A meeting was held at MSC to determine necessary action
concerning recent contamination of CM 103's potable water, oxygen, and
water-glycol lines. North American Rockwell proposed that all 103 aluminum lines
in the potable water and oxygen systems (approximately 72 segments) be replaced;
and proposed to follow a chemical flushing procedure for the water-glycol lines
to remove the aluminum oxide and copper contamination. North American estimated
that these actions would cause a 15-17 day serial impact. Removal and
replacement of all lines would result in an estimated impact of 45 days. A
decision was made to concur with the North American recommendation and on
January 19 Kenneth S. Kleinknecht, MSC, informed Dale D. Myers, North American,
of the concurrence and authorized him to proceed immediately. In addition,
Kleinknecht appointed a Special Task Team for Spacecraft 103 Contamination
Control to ensure timely review of all contractor activities associated with
removal of the contamination from the spacecraft environmental control system
coolant system. Members of the team were: Wilbur H. Gray, Chairman; A. M.
Worden, W. R. Downs, Jack Cohen, A. W. Joslyn, R. E. Smylie, R. P. Burt, and W.
H. Taylor.
On February 20 Myers notified Kleinknecht of initiation of the potable water
line changes and setting up of a monitor water-glycol system that would
duplicate CSM 103 operations during the balance of checkout and would be
examined for corrosion damage just before Flight Readiness Review.
Memo, Manager, CSM, ASPO, to Manager, ASPO, "Meeting held to determine course
of action regarding contamination of CM 103 plumbing," Jan. 19, 1968; ltr.,
Kleinknecht to Myers, Jan. 19, 1968; memo, Manager, CSM, ASPO, to distr.,
"Spacecraft Plumbing Contamination Control Board," Jan. 19, 1968; ltr., Myers to
Kleinknecht, Feb. 20, 1968.
January 18-19
Rolf Lanzkron and Owen Morris, Chiefs of MSC's CSM and LM
Project Engineering Divisions, led a review of the 2TV-1 and LTA-8 (thermal
vacuum test article and lunar module test article) thermal vacuum test programs
at MSC. Chief concerns expressed during the review centered on the heavy
concentration of testing during the summer of 1968, the need for simultaneous
operation of test chambers A and B, and the lack of adequately trained chamber
operations support personnel for dual testing. The review disclosed that
maintenance of testing schedules for LTA-8 was most unlikely, even with a
seven-day-a-week work schedule. (The central problem was the large number of
open items that had to be cleared before start of the tests.)
Note, C. C. Gay, Jr., to LeRoy Day, Jan. 19, 1968.
January 19
Apollo Program Director Samuel C. Phillips wrote ASPO Manager
George M. Low requesting that he establish and maintain a detailed comparison of
configuration differences between the CSM and LM. This comparison, Phillips
said, should include major interface differences, subsystems and components,
weight, performance, and crew safety. Phillips ordered this comparison chiefly
because the Apollo spacecraft was entering an extremely important phase to
certify the vehicles for manned flight.
Ltr., Phillips to Low, Jan. 19, 1968.
January 22
NASA launched Apollo 5 - the first, unmanned LM
flight - on a Saturn IB from KSC Launch Complex 37B at 5:48:08 p.m. EST. Mission
objectives included verifying operation of the LM structure itself and its two
primary propulsion systems, to evaluate LM staging, and to evaluate orbital
performances of the S-IVB stage and instrument unit. Flight of the AS-204 launch
vehicle went as planned, with nosecone (replacing the CSM) jettisoned and LM
separating. Flight of LM-1 also went as planned up to the first descent
propulsion engine firing. Because velocity increase did not build up as quickly
as predicted, the LM guidance system shut the engine down after only four
seconds of operation. Mission control personnel in Houston and supporting groups
quickly analyzed the problem. They determined that the difficulty was one of
guidance software only (and not a fault in hardware design) and pursued an
alternate mission plan that ensured meeting the minimum requirements necessary
to achieve the primary objectives of the mission. After mission completion at
2:45 a.m. EST January 23, LM stages were left in orbit to reenter the atmosphere
later and disintegrate. Apollo program directors attributed success of the
mission to careful preplanning of alternate ways to accomplish flight objectives
in the face of unforeseen events.
Memo, Samuel C. Phillips to NASA Administrator, "Apollo 5 Mission (SA-204
LM-1) Post Launch Report #l," Feb. 12, 1968 (MOR M-932-68-05).
January 22
Joseph G. Gavin, Jr., LM Program Director at Grumman, advised
ASPO Manager George M. Low of steps under way to attack the problem of stress
corrosion in the LM. (Low had expressed MSC's concern over this potential danger
on December 20, 1967.) While stating that he shared Low's concern, Gavin
believed that stress corrosion would not prove to be of significance to the LM
mission. However, his organization was prepared to reevaluate the LM's design
and fabrication to determine to what extent the problem could be ameliorated.
(Gavin denied that such metal corrosion could be absolutely eliminated using
present materials as dictated by weight constraints on the LM design.) Gavin
stated that he had created a special team of experienced designers and stress
analysts to review engineering design of every LM part sensitive to stress
corrosion, to review processes employed in fabrication of the LM structure, and
to review the adequacy of the company's quality control procedures to ensure
corrosion-free parts and assemblies.
Ltr., Gavin to Low, Jan. 22, 1968.
January 24
Eberhard F. M. Rees, head of the Apollo Special Task Team at
North American Rockwell, met with Kenneth S. Kleinknecht, MSC, and Martin L.
Raines, Manager of the White Sands Test Facility, to review the team's recent
operations and the responses of North American and its numerous subcontractors
to the team's recommendations. Kleinknecht listed what he thought were the chief
problems facing the CSM program: the S-band highgain antenna (which he said
should be turned over entirely to the task team for resolution); the parachute
program; the environmental control system; and contamination inside the
spacecraft. He urged that the team take the lead in developing solutions to
these problems.
Memo for Record, Raines, "Review of Apollo Special Task Team Operations,"
Jan. 26, 1968.
January 25
In a letter to officials of the three manned space flight
Centers, NASA Apollo Program Director Samuel C. Phillips called attention to the
fact that as the time for the first manned Apollo flight was approaching
constant concern for crew safety was becoming more pronounced. Phillips pointed
out that the Crew Safety Panel, Flight Mechanics Panel, Launch Operations Panel,
Hazardous Emergency Egress Working Group, and other Intercenter Coordination
Panels had each dealt with specific aspects of Apollo crew safety. Individual
Centers and contractors had exercised their crew safety responsibilities through
system design, quality control, and test channels. Single-point failure
analyses, dealing with specific hardware areas, had been made.
He said that these efforts had resulted in current provisions for rapid crew
egress on the pad, for spacecraft abort during early phases of the launch, and
for contingency flight modes. Phillips added, ". . . to insure that all of the
many parts of the problem are properly integrated we should at this time step
back and take another look at the overall crew safety picture from ingress to
mission completion. The questions to be addressed are:
- Have we systematically analyzed all likely failure modes or anomalies
which could jeopardize the crew from ingress to mission completion?
- In each of these cases do we have proper and timely cues coupled with a
safe egress, abort, or contingency capability?
- Do we have a plan for the timely solution of the known crew safety related
problems?
. . . I would like to have this essential area worked under
leadership of MSC-focused at a high management level - with assistance as
required from MSFC and KSC. . . ." In a reply to Phillips, on February 28, MSC's
George Low indicated that John Hodge had agreed to undertake the task and had
already held discussions on the subject with George Hage of Phillips' office.
Ltrs., Phillips to MSC, MSFC, and KSC, "Apollo Crew Safety Review," Jan. 25,
1968; Low to Phillips, Feb. 28, 1968.
January 26
The Special Task Team for CSM 103, appointed January 18,
submitted a progress report of activities during daily sessions held January 22
through 25. North American Rockwell and NASA had reached agreements on:
- Cleaning and flushing of water management and oxygen systems. Since all
aluminum lines except for three were replaced on CM 103 with new lines the
resolution for cleaning and flushing these systems was quickly accomplished.
- Cleaning and flushing of water glycol system.
- Pressure integrity of the water glycol system would be confirmed by a
hydrostatic check to 248 newtons per square centimeter (360 pounds per
square inch). Leak integrity would be confirmed by subsequent checks with
helium at 41 newtons per sq cm (60 psi).
- A resolution was obtained on the chemistry of the various cleaning and
flushing fluids to be used on CM 103.
- Agreement was reached on verification of cleaning and flushing all flow
paths.
The events leading to the situation on CSM 103 were
reviewed in sufficient detail to make visible the errors in the discipline
governing the flushing carts. RASPO Manager Wilbur H. Gray stated that it was
the RASPO responsibility to ensure the upgrading and control of all such
equipment which interfaced with the spacecraft. The team would convene again
January 30 to review reports and continue with other activities required to
ensure adequacy of the CSM 103 plumbing system.
Memo, Gray to distr., "Summary of progress on the Special Task Team for CSM
103 Contamination Control," Jan. 26, 1968.
January 26
A LM-2 flight and requirement meeting was held at MSC,
attended by key MSC and NASA Hq. officials. The group reached three conclusions:
- The LM-1 performance on the January 22 Apollo 5 mission had been excellent
for all conditions of the flight, as executed, with the exception of minor
anomalies.
- The LM-2 flight objectives that were partially accomplished could be
better accomplished by further ground testing or on subsequent manned
missions. Further unmanned flight testing was not required for man-rating
purposes.
- A LM-2 flight was not required to man-rate the ascent engine
injector.
It was also agreed that a decision should be made not to fly
the LM-2 mission, with this decision reversible if further evaluation of data
from the LM-1 flight indicated any problems. This decision would be reviewed at
the February 6 Manned Space Flight Management Council Meeting and on March 6 at
the LM-3 Design Certification Review. The final decision would not be made until
March 6.
Minutes of the LM-2 Flight Requirements Meeting, Jan. 26, 1968.
January 26
In response to a letter from ASPO Manager George M. Low in
late December 1967, seeking assurances that no potential stress corrosion
problems existed in the CSM, Dale D. Myers, CSM Program Manager at North
American Rockwell, reviewed the three instances where problems had been
encountered during the CSM project and iterated the extensive efforts to ensure
against such potential problems. Echoing much the same words as his counterpart
at Grumman, Myers stated that "it is not possible to guarantee that no single
instance of stress corrosion will ever occur" and that circumstances "could
create a problem not anticipated." He concluded that his company's efforts in
this direction had been "entirely adequate and beyond the requirements of the
contract and good practice in this industry," and he seated his belief that
additional efforts in this area would not produce measurable results.
Ltr., Myers to Low, Jan. 26, 1968.
January 30
MSC CSM Manager Kenneth S. Kleinknecht, in a letter to North
American Rockwell's Dale D. Myers, protested lack of North American reponse to
written MSC direction concerning parachute test vehicles. Kleinknecht pointed
out that MSC had "considerably modified our usual requirements in supporting the
boilerplate 19 task being performed for you by Western Ways, Inc. These efforts
seem to be completely negated by delayed go-ahead to Northrop Ventura for their
portion of the task. I understand that neither Western Ways nor Northrop Ventura
was given a go-ahead until January 19, 1968. The original written direction to
NR [North American] was on November 9, 1967, to provide another parachute test
vehicle (PTV) and give us an estimate of cost and schedule for another
boilerplate PTV." If the effort on the PTV had started at that time, "we would
now be able to use that vehicle rather than the bomb-type vehicles after losing
PTV No. 2. The cost and schedule for boilerplate 19 was not submitted to MSC
until later, on December 22, asking for a reply by January 2, 1968. Because of
the holiday period, this written reply was furnished on January 5, after an
investigation of the cost and schedule. The Engineering Change Proposal [ECP]
stated a completion date of May 5; however, after a request by my people to see
what could be done to improve this date, the improvement moved the Northrop
Ventura schedule from June 14 to May 24 [a Friday]. This date is three weeks
later than the date cited in the ECP and is completely unacceptable. . . ."
On February 29, Myers assured Kleinknecht that North American had proceeded
with the BP-19A task in advance of NASA full coverage. Initial partial coverage
was issued to North American on January 5, 1968. On March 14, in a letter of
commendation, Kleinknecht thanked Myers for the attention given the BP-19A
effort that made a March 15 completion by Western Ways possible. On May 27, W.
H. Gray, RASPO Manager, wrote another letter of commendation thanking North
American for completing BP-19A in time for a drop test in May 1968.
Ltrs., Kleinknecht to Myers, Jan. 30, 1968; Myers to Kleinknecht, Feb. 29,
1968; Kleinknecht to Myers, Mar. 14, 1968; Gray to Drucker, May 27, 1968.